Gust-tunnel investigation of a flexible-wing model with semichord line swept back 45° /
Thomas D. Reisert.
Description
- Language(s)
-
English
- Published
-
Washington, D.C. : National Advisory Committee for Aeronautics, 1949.
- Summary
-
An investigation was made in the Langley gust tunnel of a flexible-wing model with the semichord line swept back 45 degrees to obtain experimental data on the amount of gust-load alleviation that might be expected as a result of the wings flexing under load. The results indicated that unless adverse pitching motion could be eliminated or reduced the over-all load reduction would be small. The net reduction in bending moment, however, may be appreciable.
- Note
-
NACA TN No. 1959.
"October 1949."
- Physical Description
-
13 pages :
illustrations ;
28 cm.
Viewability
Item Link |
Original Source |
Full view
|
Technical Report Archive & Image Library
|